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Production processes at KGHM are complex and require from customers products of constantly higher quality at relatively lowest prices. Such situation results in an increase of the importance of optimisation of processes. As products and technologies change rapidly, technologists at the plant in Głogów have less time to achieve optimisation basing on own experiences. Analysing a particular process, we can e.g. detect occurring disturbances, find factors having an influence on quality problems, select optimal settings or compare various production procedures. Analysis of the course of production process is the basis of process optimisation. One optimisation in case of the process of decopperisation of flash slag can be a change of a technological additive to a less energy-consuming one, and its final result can be an improvement of the productivity index, a change of the relation between final effects and born expenditures, as well as optimisation of production costs.
Czasopismo
Rocznik
Tom
Strony
5--8
Opis fizyczny
Bibliogr. 6 poz., rys., tab., wykr.
Twórcy
autor
- Faculty of Mechanical Engineering, University of Zielona Góra, ul. Prof. Z. Szafrana 4, 65-516 Zielona Góra, Poland
autor
- Institute of Metallurgy and Materials Engineering, ul. W. Reymonta 25, 30-059 Kraków, Poland
autor
- Faculty of Mechanical Engineering, University of Zielona Góra, ul. Prof. Z. Szafrana 4, 65-516 Zielona Góra, Poland
autor
- Faculty of Foundry Engineering, AGH University of Science and Technology, Reymonta 23, 30-059 Kraków, Poland
autor
- Faculty of Foundry Engineering, AGH University of Science and Technology, Reymonta 23, 30-059 Kraków, Poland; Metallurgy Department Huta Legnica, KGHM Polska Miedź S.A., Skłodowskiej-Curie 48, 59-301 Lubin, Poland
autor
- AGH University of Science and Technology, Faculty of Non-Ferrous Metals, al. A. Mickiewicza 30, 30-059 Cracow, Poland
Bibliografia
- [1] Li, Y., Yang, S.-H., Tang, C.-B., Chen, Y.-M. He, J. & Tang, M.-T. (2018). Reductive-Sulfurizing Smelting Treatment of Smelter Slag For Copper And Cobalt Recovery. Journal of Mining and Metallurgy, Section B: Metallurgy. 54(1) B, 73-79.
- [2] Gierek, A., Karwan, T., Rojek, J. & Szymek, J. (2005). Results of test with decoperisation of slag from flash process. Ores and Non-Ferrous Metals. 50, 12, 669-680. (in Polish).
- [3] Kucharski, M., Sak, T., Madej, P. & Wędrychowicz, M. (2014). A study on the copper recovery from the slag of the outokumpu direct-to-copper process. Metallurgical and Materials Transactions. B, Process Metallurgy and Materials Processing Science. 45(2), 590-602.
- [4] Bydałek, A., Bydałek, A.W., Kurzydłowski, J. (2013). Polish Patent No. 222166, Warsaw. Republic of Poland Patent Office.
- [5] Tanaka, T. & Nakamoto, M. (2005). A Model for Estimation of Viscosity of Molten Silicate Slag. The Iron and Steel Institute of Japan International (ISIJ). 45(5), 651-656. DOI: 10.2355/isijinternational.45.651.
- [6] Ray, H.S. (2006). Theory of Toop and Samis, Introduction to Melts: Molten Salts, Slags and Glasses. Allied Publishers, New Delhi. p.104-112. ISBN: 81-7764-875.
Uwagi
PL
Opracowanie rekordu w ramach umowy 509/P-DUN/2018 ze środków MNiSW przeznaczonych na działalność upowszechniającą naukę (2018).
Typ dokumentu
Bibliografia
Identyfikator YADDA
bwmeta1.element.baztech-2bbff069-ca1a-4dde-9b7a-2b49a883daf6